Solder Paste Failure Analysis & Solutions

1. Composition & Function
- Solder Alloy Powder (85-90%): Forms electrical connections (Sn-Pb, Sn-Ag-Cu, Sn-Bi).
- Flux (10-15%): Contains activators, thixotropic agents, resins, and solvents.
2. Common Failure Causes
- Flux Overflow:
- Excessive flux (>20%) or insufficient thixotropic agent.
- Improper heating (rapid preheating causes solvent boiling).
- Oxidation & Moisture: Degrades alloy powder and flux performance.
3. Analytical Methods
- Metal Analysis (ICP-OES): Measures Sn, Ag, Cu ratios.
- Organic Analysis (GC-MS/Py-GCMS): Identifies solvents and resins.
4. Improvement Solutions
- Formula Adjustment: Reduce flux (<12%) or use high-boiling solvents.
- Process Optimization: Extend preheating (60-120s) for better solvent evaporation.
- Supplier Screening: Ensure thixotropic agent content meets standards.
Example: A smartphone manufacturer reduced flux overflow defects from 0.8% to 0.12% by adjusting flux content and preheating time, saving ¥2.3M annually.
(Note: For visual aids, include diagrams of solder paste composition, failure modes, and analytical techniques.)
Solder Paste Failure Analysis & Solutions

1. Composition & Function
- Solder Alloy Powder (85-90%): Forms electrical connections (Sn-Pb, Sn-Ag-Cu, Sn-Bi).
- Flux (10-15%): Contains activators, thixotropic agents, resins, and solvents.
2. Common Failure Causes
- Flux Overflow:
- Excessive flux (>20%) or insufficient thixotropic agent.
- Improper heating (rapid preheating causes solvent boiling).
- Oxidation & Moisture: Degrades alloy powder and flux performance.
3. Analytical Methods
- Metal Analysis (ICP-OES): Measures Sn, Ag, Cu ratios.
- Organic Analysis (GC-MS/Py-GCMS): Identifies solvents and resins.
4. Improvement Solutions
- Formula Adjustment: Reduce flux (<12%) or use high-boiling solvents.
- Process Optimization: Extend preheating (60-120s) for better solvent evaporation.
- Supplier Screening: Ensure thixotropic agent content meets standards.
Example: A smartphone manufacturer reduced flux overflow defects from 0.8% to 0.12% by adjusting flux content and preheating time, saving ¥2.3M annually.
(Note: For visual aids, include diagrams of solder paste composition, failure modes, and analytical techniques.)